Hands-on Practice NITAC Advanced Course Mechanical and Electronic System Engineering Student

Consideration of Experiment

2020-10-25
S.Takahashi

Consequence

Driving time was more improved than before session due to fixing hardware trouble.

Clearly difference of driving performance appear difinitely cause of Arduino not to be able to output high velocity settings.

Because Arduino absolutely brokes.

Future Plan

  1. Other comparison method
  2. Other driving settings
  3. Other course

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