Hands-on Practice NITAC Advanced Course Mechanical and Electronic System Engineering Student

Experiment 2

2020-10-10
S.Takahashi

Consequence

More data can be available in experiment moreover assumption.

Trouble

  1. steering wheel and dualshock3 control is not good at working on steering right.
  2. acceleration and steering input -> rc stops.

-> Arduino’s malfunction.

  1. View latency on streaming (about 400 ms)

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